[ Upstream commit df993fced230daa8452892406f3180c93ebf7e7b ]
The HVS can change AXI request mode based on how full the COB
FIFOs are.
Until now the vc4 driver has been relying on the firmware to
have set these to sensible values.
With HVS channel 2 now being used for live video, change the
panic mode for all channels to be explicitly set by the driver,
and the same for all channels.
Fixes: c54619b0bf ("drm/vc4: Add support for the BCM2711 HVS5")
Signed-off-by: Dave Stevenson <dave.stevenson@raspberrypi.com>
Link: https://lore.kernel.org/r/20221207-rpi-hvs-crtc-misc-v1-2-1f8e0770798b@cerno.tech
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit cf53db768a8790fdaae2fa3a81322b080285f7e5 ]
A problem about modprobe vc4 failed is triggered with the following log
given:
[ 420.327987] Error: Driver 'vc4_hvs' is already registered, aborting...
[ 420.333904] failed to register platform driver vc4_hvs_driver [vc4]: -16
modprobe: ERROR: could not insert 'vc4': Device or resource busy
The reason is that vc4_drm_register() returns platform_driver_register()
directly without checking its return value, if platform_driver_register()
fails, it returns without unregistering all the vc4 drivers, resulting the
vc4 can never be installed later.
A simple call graph is shown as below:
vc4_drm_register()
platform_register_drivers() # all vc4 drivers are registered
platform_driver_register()
driver_register()
bus_add_driver()
priv = kzalloc(...) # OOM happened
# return without unregister drivers
Fixing this problem by checking the return value of
platform_driver_register() and do platform_unregister_drivers() if
error happened.
Fixes: c8b75bca92 ("drm/vc4: Add KMS support for Raspberry Pi.")
Signed-off-by: Yuan Can <yuancan@huawei.com>
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Link: https://patchwork.freedesktop.org/patch/msgid/20221103014705.109322-1-yuancan@huawei.com
Signed-off-by: Sasha Levin <sashal@kernel.org>
commit 63569d90863ff26c8b10c8971d1271c17a45224b upstream.
sparse reports
drivers/gpu/drm/vc4/vc4_drv.c:270:27: warning: symbol 'vc4_dma_range_matches' was not declared. Should it be static?
vc4_dma_range_matches is only used in vc4_drv.c, so it's storage class specifier
should be static.
Fixes: da8e393e23ef ("drm/vc4: drv: Adopt the dma configuration from the HVS or V3D component")
Signed-off-by: Tom Rix <trix@redhat.com>
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Link: https://patchwork.freedesktop.org/patch/msgid/20220629200101.498138-1-trix@redhat.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit da8e393e23efb60eba8959856c7df88f9859f6eb ]
vc4_drv isn't necessarily under the /soc node in DT as it is a
virtual device, but it is the one that does the allocations.
The DMA addresses are consumed by primarily the HVS or V3D, and
those require VideoCore cache alias address mapping, and so will be
under /soc.
During probe find the a suitable device node for HVS or V3D,
and adopt the DMA configuration of that node.
Cc: <stable@vger.kernel.org>
Signed-off-by: Dave Stevenson <dave.stevenson@raspberrypi.com>
Link: https://lore.kernel.org/r/20220613144800.326124-2-maxime@cerno.tech
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 0ee5a40152b15f200ed3a0d51e8aa782ea979c6a ]
Increase the number of post-sync blanking lines on odd fields instead of
decreasing it on even fields. This makes the total number of lines
properly match the modelines.
Additionally fix the value of PV_VCONTROL_ODD_DELAY, which did not take
pixels_per_clock into account, causing some displays to invert the
fields when driven by bcm2711.
Fixes: 682e62c454 ("drm/vc4: Fix support for interlaced modes on HDMI.")
Signed-off-by: Mateusz Kwiatkowski <kfyatek+publicgit@gmail.com>
Link: https://lore.kernel.org/r/20220613144800.326124-31-maxime@cerno.tech
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 7bcb9c8d0bc9f3cab8ac2634b056c2e6b63945ca ]
vc4_dsi_encoder_disable is partially an open coded version of
drm_bridge_chain_disable, but it missed a termination condition
in the loop for ->disable which meant that no post_disable
calls were made.
Add in the termination clause.
Fixes: 033bfe7538 ("drm/vc4: dsi: Fix bridge chain handling")
Signed-off-by: Dave Stevenson <dave.stevenson@raspberrypi.com>
Link: https://lore.kernel.org/r/20220613144800.326124-17-maxime@cerno.tech
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit d1d195ce26a14ec0a87816c09ae514e1c40e97f7 ]
Most of the differences between DSI0 and DSI1 are handled through the
ID. However, the BCM2711 DSI is going to introduce one more variable to
the mix and will break some expectations of the earlier, simpler, test.
Let's add a variant structure that will address most of the differences
between those three controllers.
Reviewed-by: Dave Stevenson <dave.stevenson@raspberrypi.com>
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Link: https://patchwork.freedesktop.org/patch/msgid/20201203132543.861591-5-maxime@cerno.tech
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 3b45eee87da171caa28f61240ddb5c21170cda53 ]
The divider calculations tried to find the divider just faster than the
clock requested. However if it required a divider of 7 then the for loop
aborted without handling the "error" case, and could end up with a clock
lower than requested.
The integer divider from parent PLL to DSI clock is also capable of
going up to /255, not just /7 that the driver was trying. This allows
for slower link frequencies on the DSI bus where the resolution permits.
Correct the loop so that we always have a clock greater than requested,
and covering the whole range of dividers.
Fixes: 86c1b9eff3 ("drm/vc4: Adjust modes in DSI to work around the integer PLL divider.")
Signed-off-by: Dave Stevenson <dave.stevenson@raspberrypi.com>
Link: https://lore.kernel.org/r/20220613144800.326124-13-maxime@cerno.tech
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 517db1ab1566dba3093dbdb8de4263ba4aa66416 ]
There is little harm in ignoring fractional coordinates
(they just get truncated).
Without this:
modetest -M vc4 -F tiles,gradient -s 32:1920x1080-60 -P89@74:1920x1080*.1.1@XR24
is rejected. We have the same issue in Kodi when trying to
use zoom options on video.
Note: even if all coordinates are fully integer. e.g.
src:[0,0,1920,1080] dest:[-10,-10,1940,1100]
it will still get rejected as drm_atomic_helper_check_plane_state
uses drm_rect_clip_scaled which transforms this to fractional src coords
Fixes: 21af94cf1a ("drm/vc4: Add support for scaling of display planes.")
Signed-off-by: Dom Cobley <popcornmix@gmail.com>
Link: https://lore.kernel.org/r/20220613144800.326124-5-maxime@cerno.tech
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Signed-off-by: Sasha Levin <sashal@kernel.org>
commit db2b927f8668adf3ac765e0921cd2720f5c04172 upstream.
The dmas property is used to hold the dmaengine channel used for audio
output.
Older device trees were missing that property, so if it's not there we
disable the audio output entirely.
However, some overlays have set an empty value to that property, mostly
to workaround the fact that overlays cannot remove a property. Let's add
a test for that case and if it's empty, let's disable it as well.
Cc: <stable@vger.kernel.org>
Signed-off-by: Phil Elwell <phil@raspberrypi.org>
Link: https://lore.kernel.org/r/20220613144800.326124-18-maxime@cerno.tech
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 5453343a88ede8b12812fced81ecd24cb888ccc3 ]
If we use a format that has padding instead of the alpha component (such
as XRGB8888), it appears that the Transposer will fill the padding to 0,
disregarding what was stored in the input buffer padding.
This leads to issues with IGT, since it will set the padding to 0xff,
but will then compare the CRC of the two frames which will thus fail.
Another nice side effect is that it is now possible to just use the
buffer as ARGB.
Fixes: 008095e065 ("drm/vc4: Add support for the transposer block")
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Acked-by: Thomas Zimmermann <tzimmermann@suse.de>
Link: https://lore.kernel.org/r/20220328153659.2382206-4-maxime@cerno.tech
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 234998df929f14d00cbf2f1e81a7facb69fd9266 ]
The TXP_VSTART_AT_EOF will generate a second VSTART signal to the HVS.
However, the HVS waits for VSTART to enable the FIFO and will thus start
filling the FIFO before the start of the frame.
This leads to corruption at the beginning of the first frame, and
content from the previous frame at the beginning of the next frames.
Since one VSTART is enough, let's get rid of it.
Fixes: 008095e065 ("drm/vc4: Add support for the transposer block")
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Acked-by: Thomas Zimmermann <tzimmermann@suse.de>
Link: https://lore.kernel.org/r/20220328153659.2382206-3-maxime@cerno.tech
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 8514e6b1f40319e31ac4aa3fbf606796786366c9 ]
By default, the HVS driver will force the HVS output 3 to be muxed to
the HVS channel 2. However, the Transposer can only be assigned to the
HVS channel 2, so whenever we try to use the writeback connector, we'll
mux its associated output (Output 2) to the channel 2.
This leads to both the output 2 and 3 feeding from the same channel,
which is explicitly discouraged in the documentation.
In order to avoid this, let's reset all the output muxes to their reset
value.
Fixes: 87ebcd42fb ("drm/vc4: crtc: Assign output to channel automatically")
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Acked-by: Thomas Zimmermann <tzimmermann@suse.de>
Link: https://lore.kernel.org/r/20220328153659.2382206-2-maxime@cerno.tech
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 3d0b93d92a2790337aa9d18cb332d02356a24126 ]
If the device is already in a runtime PM enabled state
pm_runtime_get_sync() will return 1.
Also, we need to call pm_runtime_put_noidle() when pm_runtime_get_sync()
fails, so use pm_runtime_resume_and_get() instead. this function
will handle this.
Fixes: 4078f57571 ("drm/vc4: Add DSI driver")
Signed-off-by: Miaoqian Lin <linmq006@gmail.com>
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Link: https://patchwork.freedesktop.org/patch/msgid/20220420135008.2757-1-linmq006@gmail.com
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 1d118965965f89948236ebe23072bb1fca5e7832 ]
The 2711 pixel valve can't produce odd horizontal timings, and
checks were added to vc4_hdmi_encoder_atomic_check and
vc4_hdmi_encoder_mode_valid to filter out/block selection of
such modes.
Modes with DRM_MODE_FLAG_DBLCLK double all the horizontal timing
values before programming them into the PV. The PV values,
therefore, can not be odd, and so the modes can be supported.
Amend the filtering appropriately.
Fixes: 57fb32e632 ("drm/vc4: hdmi: Block odd horizontal timings")
Signed-off-by: Dave Stevenson <dave.stevenson@raspberrypi.com>
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Link: https://patchwork.freedesktop.org/patch/msgid/20220127135116.298278-1-maxime@cerno.tech
Signed-off-by: Sasha Levin <sashal@kernel.org>
Commit 20b0dfa86bef0e80b41b0e5ac38b92f23b6f27f9 upstream.
The original commit depended on a rework commit (724fc856c09e ("drm/vc4:
hdmi: Split the CEC disable / enable functions in two")) that
(rightfully) didn't reach stable.
However, probably because the context changed, when the patch was
applied to stable the pm_runtime_put called got moved to the end of the
vc4_hdmi_cec_adap_enable function (that would have become
vc4_hdmi_cec_disable with the rework) to vc4_hdmi_cec_init.
This means that at probe time, we now drop our reference to the clocks
and power domains and thus end up with a CPU hang when the CPU tries to
access registers.
The call to pm_runtime_resume_and_get() is also problematic since the
.adap_enable CEC hook is called both to enable and to disable the
controller. That means that we'll now call pm_runtime_resume_and_get()
at disable time as well, messing with the reference counting.
The behaviour we should have though would be to have
pm_runtime_resume_and_get() called when the CEC controller is enabled,
and pm_runtime_put when it's disabled.
We need to move things around a bit to behave that way, but it aligns
stable with upstream.
Cc: <stable@vger.kernel.org> # 5.10.x
Cc: <stable@vger.kernel.org> # 5.15.x
Cc: <stable@vger.kernel.org> # 5.16.x
Reported-by: Michael Stapelberg <michael+drm@stapelberg.ch>
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 20b0dfa86bef0e80b41b0e5ac38b92f23b6f27f9 upstream.
Similarly to what we encountered with the detect hook with DRM, nothing
actually prevents any of the CEC callback from being run while the HDMI
output is disabled.
However, this is an issue since any register access to the controller
when it's powered down will result in a silent hang.
Let's make sure we run the runtime_pm hooks when the CEC adapter is
opened and closed by the userspace to avoid that issue.
Fixes: 15b4511a4a ("drm/vc4: add HDMI CEC support")
Reviewed-by: Dave Stevenson <dave.stevenson@raspberrypi.com>
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Link: https://patchwork.freedesktop.org/patch/msgid/20210819135931.895976-6-maxime@cerno.tech
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit 3e85b81591609bb794bb00cd619b20965b5b38cd ]
When the firmware doesn't setup the HSM rate (such as when booting
without an HDMI cable plugged in), its rate is 0 and thus any register
access results in a CPU stall, even though HSM is enabled.
Let's enforce a minimum rate at boot to avoid this issue.
Fixes: 4f6e3d66ac ("drm/vc4: Add runtime PM support to the HDMI encoder driver")
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Reviewed-by: Nicolas Saenz Julienne <nsaenz@kernel.org>
Tested-by: Nicolas Saenz Julienne <nsaenz@kernel.org>
Tested-by: Michael Stapelberg <michael@stapelberg.ch>
Link: https://patchwork.freedesktop.org/patch/msgid/20210922125419.4125779-4-maxime@cerno.tech
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 1698ecb218eb82587dbfc71a2e26ded66e5ecf59 ]
Symptom is random switching of speakers when using multichannel.
Repeatedly running speakertest -c8 occasionally starts with
channels jumbled. This is fixed with HD_CTL_WHOLSMP.
The other bit looks beneficial and apears harmless in testing so
I'd suggest adding it too.
Documentation says: HD_CTL_WHILSMP_SET
Wait for whole sample. When this bit is set MAI transmit will start
only when there is at least one whole sample available in the fifo.
Documentation says: HD_CTL_CHALIGN_SET
Channel Align When Overflow. This bit is used to realign the audio
channels in case of an overflow.
If this bit is set, after the detection of an overflow, equal
amount of dummy words to the missing words will be written to fifo,
filling up the broken sample and maintaining alignment.
Signed-off-by: Dom Cobley <popcornmix@gmail.com>
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Reviewed-by: Nicolas Saenz Julienne <nsaenz@kernel.org>
Link: https://patchwork.freedesktop.org/patch/msgid/20210525132354.297468-7-maxime@cerno.tech
Signed-off-by: Sasha Levin <sashal@kernel.org>
commit 47a50743031ad4138050ae6d266ddd3dfe845ead upstream.
The vc4_set_crtc_possible_masks is meant to run over all the encoders
and then set their possible_crtcs mask to their associated pixelvalve.
However, since the commit 39fcb28083 ("drm/vc4: txp: Turn the TXP into
a CRTC of its own"), the TXP has been turned to a CRTC and encoder of
its own, and while it does indeed register an encoder, it no longer has
an associated pixelvalve. The code will thus run over the TXP encoder
and set a bogus possible_crtcs mask, overriding the one set in the TXP
bind function.
In order to fix this, let's skip any virtual encoder.
Cc: <stable@vger.kernel.org> # v5.9+
Fixes: 39fcb28083 ("drm/vc4: txp: Turn the TXP into a CRTC of its own")
Acked-by: Thomas Zimmermann <tzimmermann@suse.de>
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Link: https://patchwork.freedesktop.org/patch/msgid/20210507150515.257424-3-maxime@cerno.tech
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
[ Upstream commit e590c2b03a6143ba93ddad306bc9eaafa838c020 ]
Cppcheck complains that the declaration doesn't match the function
definition. Obviously "left" should come before "right". The caller
and the function implementation are done this way, it's just the
declaration which is wrong so this doesn't affect runtime.
Reported-by: kernel test robot <lkp@intel.com>
Signed-off-by: Dan Carpenter <dan.carpenter@oracle.com>
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Link: https://patchwork.freedesktop.org/patch/msgid/YH/720FD978TPhHp@mwanda
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit e075a7811977ff51c917a65ed1896e08231d2615 ]
If the of_get_named_gpio_flags call fails in vc4_hdmi_bind, we jump to
the err_unprepare_hsm label. That label will then call
pm_runtime_disable and put_device on the DDC device.
We just retrieved the DDC device, so the latter is definitely justified.
However at that point we still haven't called pm_runtime_enable, so the
call to pm_runtime_disable is not supposed to be there.
Fixes: 10ee275cb1 ("drm/vc4: prepare for CEC support")
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Link: https://patchwork.freedesktop.org/patch/msgid/20210524131852.263883-1-maxime@cerno.tech
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 9984d6664ce9dcbbc713962539eaf7636ea246c2 ]
If the HPD GPIO is not available and drm_probe_ddc fails, we end up
reading the HDMI_HOTPLUG register, but the controller might be powered
off resulting in a CPU hang. Make sure we have the power domain and the
HSM clock powered during the detect cycle to prevent the hang from
happening.
Fixes: 4f6e3d66ac ("drm/vc4: Add runtime PM support to the HDMI encoder driver")
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Reviewed-by: Dave Stevenson <dave.stevenson@raspberrypi.com>
Link: https://patchwork.freedesktop.org/patch/msgid/20210525091059.234116-4-maxime@cerno.tech
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit 411efa18e4b03840553ff58ad9b4621b82a30c04 ]
In order to access the HDMI controller, we need to make sure the HSM
clock is enabled. If we were to access it with the clock disabled, the
CPU would completely hang, resulting in an hard crash.
Since we have different code path that would require it, let's move that
clock enable / disable to runtime_pm that will take care of the
reference counting for us.
Fixes: 4f6e3d66ac ("drm/vc4: Add runtime PM support to the HDMI encoder driver")
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Reviewed-by: Dave Stevenson <dave.stevenson@raspberrypi.com>
Link: https://patchwork.freedesktop.org/patch/msgid/20210525091059.234116-3-maxime@cerno.tech
Signed-off-by: Sasha Levin <sashal@kernel.org>
[ Upstream commit eb9dfdd1ed40357b99a4201c8534c58c562e48c9 ]
Experimentally have found PV on hvs4 reports fifo full
error with expected settings and does not with one less
This appears as:
[drm:drm_atomic_helper_wait_for_flip_done] *ERROR* [CRTC:82:crtc-3] flip_done timed out
with bit 10 of PV_STAT set "HVS driving pixels when the PV FIFO is full"
Fixes: c8b75bca92 ("drm/vc4: Add KMS support for Raspberry Pi.")
Signed-off-by: Dom Cobley <popcornmix@gmail.com>
Signed-off-by: Maxime Ripard <maxime@cerno.tech>
Link: https://patchwork.freedesktop.org/patch/msgid/20210318161328.1471556-3-maxime@cerno.tech
Signed-off-by: Sasha Levin <sashal@kernel.org>